In this week, our team already finished
the final designed of the sensor mount. And we will use 3D printer to
make in the coming week. However, the corrugated metal strip we got from last
week was not idea as what we thought. Firstly, its distance between peaks was
not really accurate as we want. Secondly, the square wave shape was not good
either. Therefore, we just contacted with a 3D printer show. And we think it
will be more accurate.
Moreover, we found out another problem is
which side the strip should set on the track. At the beginning, we wanted set
it on the inner orbit. Nevertheless, we realized when the bogie get into the
parking place, the outer orbit has to have the strip. In this case, the bogie
should have both side sensor. Otherwise, we could not determine the position
when the bogie get into the parking place. So we will try to solve this program
during the coming week.
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