Wednesday, November 23, 2016

Week 11/17 to 11/23

In this week, our team already finished the final designed of the sensor mount. And we will use 3D printer to make in the coming week. However, the corrugated metal strip we got from last week was not idea as what we thought. Firstly, its distance between peaks was not really accurate as we want. Secondly, the square wave shape was not good either. Therefore, we just contacted with a 3D printer show. And we think it will be more accurate.
Moreover, we found out another problem is which side the strip should set on the track. At the beginning, we wanted set it on the inner orbit. Nevertheless, we realized when the bogie get into the parking place, the outer orbit has to have the strip. In this case, the bogie should have both side sensor. Otherwise, we could not determine the position when the bogie get into the parking place. So we will try to solve this program during the coming week.

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